Last night, my colleague Jason Torchinsky and I spent about three hours tearing apart the 170,000 mile Jeep 4.0-liter inline-six in the 1991 Jeep Cherokee that I had sold to a nice lady who had driven all the way from Chicago for a Jeep that would only take her 20 miles towards home before overheating. I was initially worried that the “unkillable” Jeep engine was toast, since it had such a severe knock, but then I learned that the noise was just the water pump banging against the engine block. Still, the engine didn’t run properly, and had no compression in the middle cylinders. So I sent an oil sample out to Blackstone Labs, who found elevated aluminum and iron content, indicating piston and piston ring/camshaft wear. The lab had found no indication of coolant in the oil, which was odd, as multiple adjacent cylinders without compression is almost always a symptom of a failed head gasket (which tends to cause coolant to leak into the oil). Maybe the head gasket wasn’t the issue, and those center pistons had somehow failed? This wouldn’t be the first time I’d heard of a Jeep 4.0 piston breaking to pieces.

I’ve lost a lot of sleep over this, since I really don’t feel like swapping an entire motor, especially not by the June 1 deadline that the buyer gave me (Yes, she still wants the Jeep, and she needs it soon). So to improve my nightly rest, Torch and I finally yanked the head off the motor yesterday. It’s a job I’ve done far too many times, as AMC’s most legendary motor is— if I’m honest — deeply flawed when used in an XJ, a vehicle with a marginal cooling system.

  A post shared by David Tracy (@davidntracy) This head extraction was easier than ever, since I had an extra set of hands and great weather on my side.

We removed the electric fan and airbox, undid the exhaust and intake manifold, took off the power steering pump, set aside the fuel injector wiring harness, popped off the spark plug wires, unbolted the thermostat and water pump (these weren’t strictly necessary to get the head off, but I’m replacing both), lifted the valve cover, and then loosened all the cylinder head bolts. From there, I slid a breaker bar into the thermostat hole in the head, and lifted up. After quite a bit of pushing, the cylinder head finally popped up, revealing my engine’s six cylinders:

Here’s a look at the engine just before head liftoff, but after we’d removed the intake and exhaust manifold (which you can see there along with the dangling injector harness), as well as the power steering pump, valve cover, thermostat, and airbox:

Here you can see the valve cover and intake manifold:

Once we had the head off, we faced the moment of truth: Would there be catastrophic damage, or was this truly just a head gasket failure? By the grace of the car gods, the pistons all looked to be in good shape, though the bridges between cylinders two and three, three and four, and four and five were all covered in coolant. You’ll also notice that there’s coolant in cylinder five, sitting atop the piston:

With coolant getting into the cylinders, and oil getting quite hot, you may wonder if there’s any damage to the cylinder walls. Let’s have a look:

Cylinder six does show a bit of vertical scoring on the cylinder wall, but touching it with my fingernail reveals that it’s quite shallow (undetectable, really). Having opened up a 4.0-liter straight six before, this isn’t that abnormal, and I don’t think it’s something to worry about. The remaining visible cylinder walls all looked nice:

Let’s have a peak at the failed head gasket:

It’s hard to tell how much of the damage occurred during cylinder head extraction, but you can see some bent fire rings (that’s the silver ring around the cylinder bore hole). The image below shows how a new gasket should look. Again, it’s hard to see exactly where the failure occurred, but it clearly did, as coolant was able to pour into the cylinders and cover the bridges between the cylinders (and this didn’t happen during head-removal, as the head was pretty much completely devoid of coolant). I wouldn’t be surprised if the head is warped, allowing coolant to travel between it and the gasket.

Anyway, the cylinder head now sits in the back of my Jeep. Tomorrow I’ll dump it off at the machine shop, where a 350 pound dude will check the thing for cracks, find them, and then I’ll be removing the head from the spare engine I have in my garage. That head will be checked and then shaved flat. Then Torch and I will reinstall it and pray that this Jeep runs like a dream so I can finally sell it, and bring my fleet down to a reasonable number of cars. I’m not sure how many exactly, which is kind of an indication that maybe it’s still too many, but let’s just ignore that.   Problem is, based on your pictures, this thing was DUMPING coolant into #5 and #6. See how they magically have no carbon buildup? That’s where all the coolant went. Into those cylinders where it steam cleaned off the crud. Where you had compression. That’s bad. Real bad. Any time you’ve got a 4.2 or 4.0 with this kind of evidence, the head is no longer a mill job. Valvetrain is non-adjustable, and popping cylinders like that alone is enough push it out. And it’s a tight spec – 040 to 060 preload, spread preferred to be under 010. Which brings us to the big problem: it was absolutely pouring the coolant into 5 and 6, and there’s no obvious indication as to why. Coolant had to come from somewhere, right? Yep. It’s the other fracture I hate on these. The one even good shops often miss because it’s only visible on x-ray, even when you pull the water plugs, and sometimes sneaks by pressure test. And it’s why you don’t have milkshake. See the coolant plug at #5? Great. Go toward #6, now you see the casting mark between #5 and #6? That’s exactly where I’d expect to find the blowout. Inside the head. Pull the #5 water plug (carefully!!) with the head set up so that you can see the underside as well. (Yeah, it’s a little tricky.) It’s definitely best if you can block up the water jackets and let it sit a while. You’ll be looking for any water at all on the #5 and #6 valves. Exhaust or intake. Any trace of water on the valves, the head is a core. Don’t waste time welding. “But I have no milkshake, this makes no sense!” Ah, but it does. The 4.0 runs hot, especially in back. Those cylinders got a steam cleaning, and because the block was extra hot due to a (likely coincidental) water pump failure, the pistons were sealing up very well. So the coolant was held in chamber well, and flashed to steam, giving you nice shiny pistons. And there’s absolutely no contact with oil except within the bore, where it’s being flashed to steam and out the exhaust. Prep the other head now, come back to this one later. I suspect you can get an article on X-ray NDT of heads out of it. I’ve got two heads ready to rock. The more I think about it though, the more I’m suspecting the head was already fractured at #5-#6 and the water pump was incidental. (So hooray for that timing.) Those cylinders are not 25 miles clean, they’re 250+ miles clean. There’s also some evidence of steam in #2 so it might have two cracks. Plus the warping. Still, it was caught before hydrolock or thrown rod. So overall, the bottom end is better than fine. I mean hell, two clean cylinders. May as well grab a breaker bar and some brill-o while waiting and do the other four. 😉 (Joking. Get some Orison Piston Kleen though. Follow directions for mixing, lower pistons from TDC, let it soak, get as much out as you can after 24 hours, and add some oil to bores before rotating.) There’s a shitload of gunk in the coolant channels though, and unevenly distributed as usual. I would absolutely do two flushes (disconnect the heater core) with Mopar 4856977AB – accept absolutely no substitutes, it’s literally the only one I use for all makes and models. Should be about $12-15 at any dealer. Because it works, and it works well. Plus at least one tap water flush after. Depends how bad the Jeep(R)-brand Coolange(TM) Sluj(R) coming out is. Very common problem on these, but if left unaddressed, can cause premature water pump failure and worse. Especially any jackets are fully clogged – believe me, it happens. What does bug me about this one is that there’s evidence of coolant in the cylinders everywhere but where the head warped, and it’s long term. That tiny bit of rust there (doesn’t affect operation) is proof that water sat on the piston. And it’s on the high, not the low. But I’m going with the assumption that it’s from this failure and it’s head seep, since the car did sit for some time after. So the head might not mill at all. So the question then is: where’d the coolant come from and why didn’t it produce noticeable white smoke? We’re burning coolant with nothing worse than cold winter start puffs observed, unless David’s also blind. And I doubt that. This also definitely isn’t a porous casting fault. Those fail sooner, and guarantee milkshake because they dump coolant straight into oil. But something has been causing coolant intrusion into multiple cylinders over a long period. I mean, it’s better than my first concern, which was a fractured bore. Those very much do happen. So where’s the damn coolant coming from!? Without inspecting the engine in person (sorry David, I can’t make it up tonight,) it’s all EWAGs (Educated Wild-Ass-Guesses) based on experience and knowledge. Like the head bowing. But the conditions here aren’t something I’ve seen before. #5 and #6 there, absolutely. But 1, 2, 5, 6? With no white smoke? Nope. I just have not seen that. Only thing I can guess is that the head has multiple failure points and has been silently seeping coolant into the bores for a very, very, very long time. Probably only while the system’s under pressure. Not enough to affect operation or drain coolant noticeably, but enough that over a very long period, it produced nice shiny pistons. We’re talking hundreds, possibly thousands of miles of little white puffs just slowly, methodically eating up the carbon. If you catch it very early, you’ll have ‘spotty’ piston cleaning. Nothing like these – I honestly was going to ask David if he replaced pistons in this car before selling it. They’re that clean. But again: that’s 100% a guess. I do trim some of the excess threads off the top of bolt 14 so I can insert the bolt after the head is in place – I’ve never had any luck holding it up with tape. With my current pickup, it’s set so far down in the gigantic engine bay meant to accommodate 454s, it’s really a challenge at times. For example: 400 count at Costco is $40 ! but that only works out to $.10 for each glove. Worth it! https://www.costco.com/kirkland-signature-nitrile-exam-gloves%2C-400-count.product.100497804.html LOL! Yep, there it is 🙂 Glad it was relatively good news upon teardown! “vehicles placed strategically around his property.” don’t you mean — vehicles placed haphazardly around his property. I know you love that inline 6, but could you love it more with more power? It might make for a fun project (cough, cough, CONTENT, cough, cough). Does the person who bought it before have any interest in it? Just curious if she wants it or has washed her hands of it. This was right below a picture of Tracy and Torch mugging for a selfie with greasy hands, so likely you were reading in a trance at that point. I have wired more than 1 XJ electric fan to a toggle switch because the thermostat controlled switch failed. This works best for people who understand the importance of watching temperature. One, the worst cooling issues absolutely cannot be fixed. Because they’re inherent to the block. The 4.2/4.0 is a wet block mounted longitudinally. That means no matter what you do, as you move toward the rear of the engine, you are running hotter. Simply because the water pump and fan are at the front. That’s not touching on any other design issues (I’m sure they’re there, I just don’t know them.) Two, the second largest problem is that the system is extremely prone to sludging, especially when they switched to HOAT. I :heart: Mopar 6977AB because of the 4.0’s. That sludging means a very poor coolant-metal interface and reduced flow through jackets. Many times, a slightly hot running 4.0 can be fixed by doing nothing more than a very thorough chemical flush. You can see on David’s pictures a mix of white corrosion (minor issue) and grayish goop along the inside. That’s Coolange(TM) Sluj(R); a melange of iron oxide, water, glycol, oil, rubber, and plastics. Awful, radiator killing shit. Now, on the heat soak problems, I’m going to refer you to item #1. Once you’re shut down, fans or no fans, you cannot effectively remove heat from the rear of the engine. That’s why #6 is always scored. In order to fix the heat soak, you need to remove heat from the back of the engine. The water pump does a tolerable but not great job of circulating – when it’s running. So fans are largely placebo, because you’re not actually moving the heat. If I was going to attempt to solve, my solution would be frankly, extremely drastic and wildly different from anything David came up with. Because I wouldn’t touch the radiator or fans at all. I’d yank the water pump from the front, the #5 (rearmost) freeze plug permanently, tap that freeze plug, and switch to a rear-to-front flow. Remember, the back of the block will always be hottest because it’s furthest from airflow and closest to exhaust. So that’s where I’d want the coldest coolant with the highest exchange rate. It’s also a very clear illustration as to why I think it’s unsolvable. Sure, we’re gonna mount our water pump right where our intake and exhaust go. That’s definitely gonna work! Well, okay we’ll just put a 90 on it and… oh… we still have nowhere to put the pump because that’s where the power steering goes and we don’t have room. Well we could put it below, but then how are we getting water out? Oh, and how are we keeping the hot exhaust and catalytic converter from melting the water inlet? Said another way, if the problem was caused by inline longitudinal engines with mechanical water pumps being prone to overheating, why dont they all blow? Slant 6. Cummins. Every semi truck. I only ever owned one 4.0. It came to me with a blown head gasket, and I sold it with a blown head gasket. It got a bit confusing at the end.You’re planning to use another head ,but are getting the original crack tested out of curiosity?

Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 92Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 72Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 13Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 4Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 4Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 10Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 53Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 59Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 20Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 13Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 36Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 85Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 37Remember That Jeep Cherokee That Blew Up After I Sold It To A Nice Lady  I Just Took Apart Its Engine  Here s What I Found - 55